Laserfiche WebLink
SUBSEQUENT WORK REPORT <br /> Operator Amerada Petroleum Corporation Field Tracy Gas <br /> Well No. F.D.L. #1 Section 151 T. 2S., R. 5 E. M.D.B. & M. <br /> 12-29-46 Removed Xmas Tree. Tubing stuck. Could not pull loose while circulating. <br /> 12-30-46 Ran Ford Alexander line and shot off tubing in bottom collar at 40421 . <br /> Shot did not free tubing. <br /> Ran second shot and fired in third collar from bottom at 39861. Tubing <br /> free. <br /> Cement Plug #1Abandon ,5986'-3868',. Halliburton Cement Company pumped <br /> in 85 sacks of construction cement through 2-" E.U. tubing and followed <br /> • with 129 cu, ft, of mud. Plugged 13-3/8" casing from 3986' to 38681 . <br /> Pulled tubing out of hole. <br /> 1-1-47 Ran McCullough Magnatector and located free point in 13-3/8" casing <br /> at 12501 . <br /> Ran Ford Alexander line and shot off. 13-3/8" casing in collar at 12381 . <br /> 1-2&3-47 Pulled 13-3/811 casing from 12381 . <br /> 1-4-47 Cement Plug_#2 (Abandon) 1244'-12021_. Used a dump bottom bailer and <br /> pushed a 14"x14"x81 wooden block down 18-5/8" casing to stub of 13-3/8" <br /> casing at 12381. Mixed 68 sacks of construction cement and plugged <br /> 13-3/8" casing stub and 18-5/8" casing from 1244+-12021 . Placed cement <br /> with a dump bottom bailer. <br /> Plug held weight of bailer. <br /> 1-7-47 Welder cut off base plate and welded steel plate over 18-5/8" casing. <br /> WELL ABANDONED. <br />