My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
SR0085382 (4)
Environmental Health - Public
>
EHD Program Facility Records by Street Name
>
M
>
MAIN
>
2085
>
2900 - Site Mitigation Program
>
SR0085382 (4)
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
10/19/2022 9:42:54 AM
Creation date
10/19/2022 9:35:33 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
WORK PLANS
RECORD_ID
SR0085382
PE
2903
FACILITY_ID
FA0025625
FACILITY_NAME
BUGGY BATH CAR WASH / FORMER ARCO STATION NO 0559
STREET_NUMBER
2085
Direction
E
STREET_NAME
MAIN
STREET_TYPE
ST
City
STOCKTON
Zip
95205
APN
15310210
ENTERED_DATE
6/8/2022 12:00:00 AM
SITE_LOCATION
2085 E MAIN ST
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
Scanner
SJGOV\tsok
Tags
EHD - Public
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
34
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
Project Name Well Number <br /> Former Arco 559 Monitoring Well Construction Log MW-1 <br /> Address Drilling Contractor Ground Surface Elevation: Top of Casing Elevation: <br /> 2085 East Main Street Cascade Drilling 22.01 21.60 <br /> Drilling Method Boring Depth Boring Diameter <br /> Stockton California Air Knife/Hollow Stem Auger 45 ft. 8.25 in. <br /> Logged By Approved By Sampling Method Well Depth Casing Type Well Screen Interval Slot Size <br /> S.Harrington R.Bussard Split Spoon 45 ft. 2"SCH40 PVC 25-45 ft. 0.010 <br /> Antea Group Project Number Headspace Monitoring Device Date Drilling Started Date Drilling Completed <br /> BPSTOCK191 PID 12/17/2019 1/8/2020 <br /> LITHOLOGY SAMPLING DATA <br /> U C <br /> C 2 C CL N L 00 (O N J <br /> O r <br /> Graphic CO Visual o o a ° 3 o Q Well Well a <br /> W Log Cn Description 2 U _ � 0 m m J Diagram Details o <br /> No Recovery <br /> -5 <br /> 2"SCH40 PVC <br /> with 0.010 <br /> Silty Sand;brown,75%fine sand,25% Screen: <br /> ■ ■ SM non-plastic fines,non-cohesive 28.5-30 100 6 25-45 ft. <br /> • • • SP Poorly Graded Sand;green-grey,95% moist 17.4 8 <br /> 30 ML fine sand,5%fines,non-cohesive, 62.4 14 30 <br /> heavy odor <br /> Silt;green-grey,90%fines,10%fine s <br /> sand,non-plastic,cohesive <br /> -10 No Recovery <br /> CL Lean Clay with Sand;grey 33.5-35 100 7 <br /> green/brown,90%fines,10%fine wet 10 <br /> 35 sand,low-medium plasticity,cohesive 228.1 16 35 <br /> No Recovery <br /> -15 <br /> CL Lean Clay;grey with chunks of red moist 38.5-40 100 7 <br /> (oxidation),90%fines,10%fine sand, 9 <br /> 40 low plasticity,heavy odor 159.5 15 40 <br /> No Recovery <br /> -20-- <br /> CIL Lean Clay;grey/brown,95%fines,5% 43.5-45 100 8 <br /> fine sand,medium plasticity,cohesive, 15 <br /> 45 some odor moist 77.8 17 45 <br /> Boring terminated at 45 ft.bgs. <br /> -25-- <br /> 50 L L 50 <br /> SS=Split Spoon Q <br /> antea®group <br /> Page 2 of 2 77 First Encountered Groundwater 3E Static Groundwater XINOGEN® <br />
The URL can be used to link to this page
Your browser does not support the video tag.