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S A N J 0 A Q I I I Irl Environmental Health Department <br /> CCUNT <br /> Underground Storage Tank Program Inspection Report <br /> Facility Name: Facility Address: Date: <br /> KESAR PETROLEUM INC T717 W EIGHTH ST, STOCKTON March 15, 2023 <br /> Single-Walled Non-Pressurized Piping <br /> 404 CCR 2643(e),2661(f) Failure to conduct 0.1 gph test on single-walled gravity piping biennially or post repair(pre-1984) ❑V ❑R ❑COS <br /> Other Violations <br /> 2010 See below Unlisted General violation ❑V ❑R ❑COS <br /> SUMMARY OF VIOLATIONS <br /> (CLASS I,CLASS II,or MINOR-Notice to Comply) <br /> Item# Remarks <br /> 208 CCR 2716(a-e) Failure to comply with the designated operator inspection requirements. <br /> OBSERVATION: The designated operator failed to check and note the correct test dates for the secondary <br /> containment and overfill prevention on the designated operator inspection reports.The secondary containment test <br /> date was listed as 3/15/22.The correct date for the secondary containment is 3/29/23. The overfill prevention date <br /> was missing in some reports and was listed incorrectly as 3/15/22 in others.The correct overfill prevention date is <br /> 5/3/22. <br /> REGULATION GUIDANCE: During the inspection, the designated operator shall check that all required testing and <br /> maintenance for the UST system have been completed and document the dates they were done. <br /> CORRECTIVE ACTION: Ensure that designated operators performing inspections at this facility are including all of <br /> the required information on the reports. <br /> This is a repeat violation, Class II. <br /> 307 HSC 25290.1(c3), 25290.2(c3) Failure to keep water out of the secondary containment system (post-Jul 2003). <br /> OBSERVATION:Water was found in the following locations: <br /> -87-grade fill sump. <br /> -UDC that contains a black metal cover. <br /> REGULATION GUIDANCE: Secondary containment shall be constructed to prevent any water intrusion into the <br /> system by precipitation, infiltration, or surface runoff. <br /> CORRECTIVE ACTION: The service technician removed 1.5 gallons of liquid from the 87-grade fill sump and <br /> returned the sensor to its proper location. Immediately contact a properly licensed,trained, and certified contractor <br /> to address the water intrusion into the 87-grade fill sump under permit and inspection of the EHD. <br /> This is a repeat violation, Class II. <br /> 317 CCR 2636(f)(2) Failure of the line leak detector to detect a 3.0 gph leak at 10 psi and restrict or shut off flow. <br /> OBSERVATION: The 91-grade VMI line leak detector failed to detect a leak when tested. <br /> REGULATION GUIDANCE:All line leak detectors shall be capable of detecting a 3-gallon per hour leak at 10 psi. <br /> CORRECTIVE ACTION: This was corrected on site. The service technician adjusted the leak detector, retested it, <br /> and it passed. <br /> This is a Class II violation. <br /> FA0015274 PR0522448 SCO01 03/15/2023 <br /> EHD 23-01 Rev.12/06/2021 Page 4 of 5 Underground Storage Tank Program OIR <br /> 1868 E. Hazelton Avenue I Stockton, California 95205 1 T 209 468-3420 1 F 209 464-0138 1 www.sjgov.org/EHD <br />