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Mr Michael Infurna <br /> Page 2 <br /> Samples were collected after the physical parameters had stabilized and water levels had recovered to <br /> at least 99% of pre-purge levels Purge water was contained in appropriately labeled DOT-approved <br /> 55-gallon drums The drums are currently being stored onsite Purge logs are included in Attachment <br /> A <br /> Groundwater samples were delivered under chain of custody protocol to Argon Laboratories (ELAP <br /> #2359) for the analysis of BTEX using EPA method 8020, TPHg and TPHd using modified EPA <br /> method 8015, and gasoline oxygenate additives using EPA method 8260 <br /> Monitoring Well Surveying <br /> As required by AB 2886, all monitoring wells were surveyed by a Registered Surveyor to a <br /> horizontal accuracy of less than one meter and a vertical accuracy of 0 01 feet In January 2002, <br /> Morrow Surveying surveyed the latitude and longitude of the site wells relative to the North <br /> American Datum (NAD83), and surveyed the wellhead elevations relative to City of Stockton <br /> Benchmark No 186/Cal-Trans Benchmark No RM 90 A site map showing monitoring well <br /> locations, latitude and longitude coordinates and wellhead elevations is included in Attachment B <br /> Groundwater Analytical Results <br /> . 1,2 DCA and EDB continue to be at non-detectable levels in wells MWI through MW3, and no <br /> detectable concentrations of TPHg, TPHd, BTEX, or gasoline oxygenate additives were present <br /> in wells MW l and MW2 <br /> In well MW3, benzene was not detected, and no gasoline oxygenate additives were detected <br /> except for MTBE, which was detected at a concentration of 1,300 parts per billion (ppb) TPHg <br /> was detected at a concentration of 500 ppb, and TPHd was detected at a concentration of 460 <br /> ppb Analytical results are summarized in Table 2 Attachment C contains laboratory reports and <br /> chain of custody documentation <br /> Summary <br /> Groundwater levels at the site rose since the previous round of sampling During this quarter <br /> groundwater flow remained in an east-northeasterly direction, however, flow direction at the <br /> site has historically been inconsistent <br /> 1,2 DCA and EDB have not been detected in wells MW I through MW3 since sampling <br /> began TPHg, TPHd, BTEX and gasoline oxygenate additives continue to be at non- <br /> detectable levels in wells MW1 and MW2, and benzene was not detected in well MW3 <br /> TPHd and TPHg in well MW3 appear to have formed decreasing trends while MTBE <br /> concentrations are consistent with historical analytical results <br /> Benzene levels at the site continue to be less than the established maximum contaminant levels <br /> (MCL) for drinking water <br /> Woolsey chtlgmrllgrn2002 doc <br />