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VAPOR RECOVERY RESULTS ..' <br /> As of March 15, 1993, the total system has recovered'. a calculated <br /> total of 16967 poundsof hydrocarbons, 3851 of which have been ' ' <br /> produced since the beginning of operations under the; Authority to 'F <br /> Construct . <br /> As of July 21, 1992, the date it was destroyed, P1'phad. produced <br /> 2 . 96 pounds of hydrocarbons or an additional 1 . 63 ;, pounds since; <br /> the beginning of .operation under the Authority to Construct . See <br /> Table 1 . <br /> VSB5 was added to vapor: extraction well P3-Swarm on, 7/27/92 . The <br /> swarm in combination with VSB5 has produced, as of 03/15/93 , 792 <br /> pounds of hydrocarbons, ! an additional 230 pounds since operation <br /> under the Authority to Construct, VSB5 is currently producing '� r <br /> 0 . 92 pounds per day, see Table 1 . On 8/26/92, the ! P3'-Swarm was F <br /> disengaged from the vapor extraction system. <br /> Before being shut down on 7/24/92, vapor extraction:' well EX ? i <br /> produced 131 . 31 pounds of hydrocarbons, 4 . 18 pounds �'of which were <br /> produced under the Authority to Construct, see Table :l . . <br /> As of August 26, 1992,p MW1 had produced a total of 2534 pounds, <br /> of which 69 . 75 pounds have been produced during operations under a <br /> the Authority to Construct . MW1 was shut down on 7/24/92 . <br /> As of March 15, 1993 , MW5 has produced a total of 10122 pounds, of <br /> which 1727 pounds .have been produced during operations under the ., { <br /> Authority to Construct MW5 was transferred to usd as a ' clean I,} <br /> air injection well on 7/24/92 . On 7/27/92, MW5 was shutdown as an <br /> air injection well . MW5- was again hooked up as a vapor extraction <br /> well on 8/03'/92 . c i' <br /> On July 27, 1992, VSB3 , VSB9 and VSB11 were added to the system. <br /> As of March 15, ;1993 , these wells had produced the" 'Uollowing <br /> amounts of gasoline : VSB3 , 23 . 78 pounds; VSB9, 1067 ;lpouz'ds; and 4. <br /> as of 2/23/93 VS211, 370 .4 pounds. <br /> Monitor well, MW 3 has not been used for vapor extraction during <br /> the operations under the Authority to Construct . a <br /> li <br /> Currently the site is producing 8 . 73 pounds perl� !,day of TFH `s <br /> hydrocarbon. The current CO2 emission 'rate indicates that <br /> approximately 65 lb of hydrocarbon are being destroyed per day by 'k <br /> means of in-situ biological and/or chemical oxidation. <br /> If you have any questions, please call (916) 668-5300 . , <br /> Geologist <br /> J� cc : Ms . Mary Meays, San Joaquin County Health <br /> Ms . Teresa Stuyt, San Joaquin Valley Air Quality <br /> i <br /> page 6 of R604 , 04/07/93 <br /> ii, <br /> t <br />