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M <br /> I <br /> I <br /> f RESULTS <br /> See Table 1 for results influent/effluent monitoring of the system. <br /> and Table 2 for the results of REMOX operation. <br /> CONCLUSIONS r <br /> kThe VOC emissions during current REMOX operations for the period <br /> 10/10/91 to 11/05/93, have not exceeded the 52 lb/day limit. No DCE, <br /> TCE or PCE has been detected in the samples . <br /> E <br /> The average Natural Gas usage to 7/20/92 was 2 . 2 cfm, or 3168 cf <br /> per operational day, following the exchange of the. unit on. <br /> 8/18/92 the average Natural Gas usage to 11/04/95 was 5 . 28 cfm' <br /> or 7607 cfd. Since the replacement of the burner on 11/05/93 the <br /> natural gas average natural gas usage is 3 . 86 cfm or 5561 cfd <br /> which is below the permit limit of 17, 280 cfd. <br /> 1 <br /> A total of 72087 pounds of gasoline have been destroyed during <br /> operation of the vapor recovery system. <br /> The system was destroying, as of 12/07/93 , 21 . 83 lb/day of <br /> hydrocarbon. <br /> 49/u�lr i <br /> Geologist <br /> CC. <br /> { Gary Reeves <br /> San Joaquin Valley Unified Air Pollution Control District <br /> 4230 Kiernan Ave . #1.30 <br /> Modesto, CA 95356 <br /> (209) 545-7000 <br /> I <br /> Mary F. Meays <br /> Public Health Services <br /> 4 P.O. Box 2009 <br /> Stockton, California 95201 <br /> I <br /> I <br /> page 6 of R603 , 12/16/93 <br />