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PR0009051
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SITE INFORMATION AND CORRESPONDENCE
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Last modified
2/5/2020 12:26:47 PM
Creation date
2/5/2020 10:23:06 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
SITE INFORMATION AND CORRESPONDENCE
RECORD_ID
PR0009051
PE
2960
FACILITY_ID
FA0000649
FACILITY_NAME
FORMER NESTLE USA INC FACILITY
STREET_NUMBER
230
STREET_NAME
INDUSTRIAL
STREET_TYPE
DR
City
RIPON
Zip
95366
APN
25938001
CURRENT_STATUS
01
SITE_LOCATION
230 INDUSTRIAL DR
P_LOCATION
05
P_DISTRICT
005
QC Status
Approved
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Mr. Mike Desso • <br /> -2 - 3 November 2009 <br /> Nestle USA Inc. <br /> dependant on the flow modeling, but not confirmed by monitoring wells. Central Valley Water <br /> Board staff concluded that the two proposed wells in the Well Work Plan needed to be <br /> relocated to confirm that the side-gradient extent of the capture zone encompasses the entire <br /> width of the site as predicted by Nestle modeling. During the 22 October conference call, staff <br /> expressed concern that the locations proposed in the Well Work Plan were too close to the <br /> center of the predicted plume. Following the call, ECM addressed staff concerns in the <br /> 2 November 2009 addendum to the Well Work Plan that relocated the proposed wells. <br /> Industrial Avenue Site Treatment System <br /> The System Work Plan proposes to temporarily discontinue pumping of groundwater in one of <br /> the two extraction wells at the former NestlB facility. Currently, the extraction wells are both <br /> pumped at 30 gallons per minute (GPM) for a system total of 60 GPM. Pumping of EU-3 <br /> would be stopped and EU-4 would continue to be pumped at 30 GPM. The stated purpose is <br /> to determine if a zone of relatively stagnant or slow moving groundwater with elevated <br /> concentrations of trichloroethylene (TCE) exists between the extraction wells. Nestle has <br /> predicted the existence of this zone by modeling groundwater flow. Central Valley Water <br /> Board staff concludes that the proposal is not acceptable because it may reduce the onsite <br /> capture zone area by approximately 35 percent and increase the mass of TCE migrating <br /> offsite. Staff does not object to system modifications that would remove TCE within a stagnant <br /> zone provided that it is accomplished without reducing the capture zone area. <br /> Our estimate of capture zone area reduction is based on the System Work Plan model outputs <br /> presented as Figures 3 and 4; our concern regarding offsite TCE migration is highlighted by <br /> the recent arrival of TCE at monitoring well M-10A, located approximately 1,050 feet directly <br /> down-gradient of the Industrial Avenue site. The TCE concentration trend in M-1 OA between <br /> June 1988 and April 2009 is graphed on the attached figure. <br /> Stockton Avenue Site Monitoring Wells <br /> The Well Work Plan proposes the installation of two monitoring wells near the former sewer <br /> line leak at 519 South Stockton Avenue. The stated purpose of the wells is to evaluate the <br /> extent of influence of the groundwater extraction system in the C Zone, 143 to 158 feet <br /> beneath the surface. The current site conceptual model (SCM), prepared by AMEC in January <br /> 2009, concludes that concentrations of TCE and other constituents of concern within the C <br /> Zone at the Stockton Avenue site are the result of migration from the City sewage treatment <br /> ponds near the Stanislaus River, and not the result of a sanitary sewer leak in <br /> South Stockton Avenue. Therefore, Central Valley Water Board staff believes that the purpose <br /> of the proposed wells should be to verify this conclusion by comparing concentrations in the <br /> new wells with concentrations in B Zone wells near the sewer leak and with concentrations in <br /> C Zone wells that monitor the plume emanating from the sewage ponds. <br /> The SCM concludes that concentrations of TCE in the B Zone beneath 519 South Stockton <br /> Avenue are the result of a sewer line leak. Therefore, an investigation should be conducted on <br /> groundwater within the B Zone to confirm that concentrations of TCE and other constituents of <br /> concern resulting from the sewer line leak have been sufficiently reduced to justify shutdown of <br /> the treatment plant. <br />
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