My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
ARCHIVED REPORTS_XR0004464
EnvironmentalHealth
>
EHD Program Facility Records by Street Name
>
M
>
MAIN
>
341
>
2900 - Site Mitigation Program
>
PR0506186
>
ARCHIVED REPORTS_XR0004464
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
3/6/2020 4:14:33 PM
Creation date
3/6/2020 1:43:20 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0004464
RECORD_ID
PR0506186
PE
2950
FACILITY_ID
FA0007258
FACILITY_NAME
RIPON SHELL
STREET_NUMBER
341
Direction
E
STREET_NAME
MAIN
STREET_TYPE
ST
City
RIPON
Zip
95366
APN
26114007
CURRENT_STATUS
01
SITE_LOCATION
341 E MAIN ST
P_LOCATION
99
P_DISTRICT
005
QC Status
Approved
Scanner
SJGOV\sballwahn
Tags
EHD - Public
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
76
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
C A M B R I A <br /> APR S R 2005 <br /> Aril 8,2005 r �' <br /> ENVIRONMENT HEALTH p <br /> Ms Vicki McCartney PERMIT/SERVICES <br /> San Joaquin County Environmental Health Department <br /> 304 East Weber Avenue, 3rd Floor <br /> Stockton, California 95202 <br /> Re Groundwater Monitoring Report- First Quarter 2005 <br /> Shell-branded Service Station <br /> 341 East Main Street <br /> Ripon,California <br /> SAP Code 135816 <br /> Incident No 98995874 <br /> SJCEHD Site Code 506186 <br /> Dear Ms McCartney <br /> Cambria Environmental Technology, Inc (Cambria) is submitting this groundwater monitoring <br /> report on behalf of Equilon Enterprises LLC dba Shell Oil Products US (Shell) in accordance <br /> with the quarterly reporting requirements of 23 CCR 2652d <br /> FIRST QUARTER 2005 ACTIVITIES <br /> Blaine Tech Services, Inc (Blaine) of San Jose, California gauged and sampled selected wells <br /> and prepared a summary table of field gauging and laboratory analytical data Cambria prepared <br /> an area well survey map (Figure 1) and a groundwater contour/chemical concentration map for <br /> the deep zone (Figure 2) and for the shallow zone (Figure 3) Blaine's report, presenting the first <br /> quarter 2005 laboratory report, supporting field notes, and the additional December 2004 and <br /> February 2005 monthly sampling results for well MW-6A are included as Appendix A <br /> GROUNDWATER REMEDIATION <br /> Interim Groundwater Remediation: Blaine began weekly purging of onsite monitoring well <br /> MW-1 on November 10, 1998 and onsite extraction well EW-1 on March 11, 1999 This practice <br /> continued until the groundwater extraction (GWE)system was started during March 2000 <br /> Groundwater Remediation System Operation. Cambria installed a GWE system at this site <br /> which began operation in March 2000 and was shut down in July 2001 Hydrocarbon and MTBE <br /> Cambria I . ,. ..�T�,- <br /> Emironmental (.0nl.ClllYAU0ilS IId YC DCCII WDSLdIIUdlly 1CULIL,CU 1.11 gIL)UIIlWdlC1 MilUddi U1C SCLC '111G uYrl. <br /> nology,inc system extracted groundwater from well EW-1 at approximately five gallons per minute An <br /> estimate of contaminant mass removed by the GWE system is summarized in the following table <br /> 270 Perkins Street <br /> Sonoma CA 95476 <br /> Tel(707)935-4850 <br /> Fax(707)935-6649 <br />
The URL can be used to link to this page
Your browser does not support the video tag.