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r <br /> 15 December 2000 <br /> • AGE-NC Project No 95-0103 <br /> Page 4 of 4 <br /> Following casing removal,the probe borings will be permanently sealed to prevent vertical migration <br /> of contaminants Soil borings shall be abandoned by backfilling with portland from the total depth <br /> to surface grade <br /> 32 GROUND WATER EXTRACTION TESTS <br /> Two drawdown pilot tests will be performed to evaluate feasibility of ground water extraction and <br /> to remove hydrocarbon mass through ground water extraction and to reduce ground water levels to <br /> enhance soil vapor extraction A downhole water pump will be utilized to induce a decline in static <br /> water level in the extraction well, pressure transducers will be deployed in surrounding wells to <br /> measure difference in ground water levels before well pumping and at set time intervals during well <br /> pumping <br /> A ground water test will be conducted to extract water from the vapor extraction well(VE-6), ground <br /> water level observations will be collected from two temporary ground water depth/elevation <br /> monitoring points, soil vapor extraction wells VW-1 and ASO-1, and possibly from ground water <br /> monitoring well MW-3 r <br /> A second ground water tests will be later conducted to extract water from the monitoring well (MW- <br /> 4) ground water level observations will be collected from one temporary ground water <br /> depth/elevation monitoring point, soil vapor extraction wells VW-7 and VE-1, and possibly from <br /> ground water monitoring well MW-1 <br /> The ground water will be extracted utilizing a submersible, 2-inch diameter Grundfos Rediflow self- <br /> priming downhole pump The ground water pumping rate will remain constant to achieve the <br /> optimum pumping rate for the greatest drawdown influence During the pumping, the estimated <br /> ground water extraction flow rate be one-gallon per minute The ground water extraction pilot test <br /> will be performed for 24 hours to allow for stabilization of ground water drawdown <br /> Purged ground water will be containerized in a 9 000-gallon Baker tank, four ' grab" ground water <br /> samples will be collected from the inlet to the Baker tank for analysis for TPI-I-g, BTEX and MTBE <br /> in accordance with appropriate method <br /> The purged ground water will be discharged into the City of Stockton sewer system pending <br /> regulatory approval or be transported to a suitable hazardous waste facility <br /> The duration of the initial drawdown pilot test will be a minimum of 24 hours The proposed <br /> drawdown pilot test will be designed to obtain general aquifer characteristics hydraulic conductivity <br /> transmissivity well effectiveness (efficiency) and drawdown at a steady pumping rate <br />