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SITE INFORMATION AND CORRESPONDENCE
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Last modified
4/3/2020 2:10:20 PM
Creation date
4/3/2020 1:50:02 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
SITE INFORMATION AND CORRESPONDENCE
RECORD_ID
PR0524190
PE
2965
FACILITY_ID
FA0016241
FACILITY_NAME
STOCKTON REGIONAL WATER CONTROL FAC
STREET_NUMBER
2500
STREET_NAME
NAVY
STREET_TYPE
DR
City
STOCKTON
Zip
95206
APN
16333003
CURRENT_STATUS
01
SITE_LOCATION
2500 NAVY DR
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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EHD - Public
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Stockton RWCF, Tertiary Plies, -2- J 14 February 2001 <br /> Inspection Report <br /> recirculation gate valve is non-disinfected wastewater from Pond 4 and the recirculation ditch. The <br /> elevation of this wastewater is typically lower than that in the CCC unless there are conditions such as a <br /> low tide as was observed on the morning of 7 December 2000. <br /> Once the leaking was discovered, RWCF staff attempted to further close the recirculation gate valve. It <br /> was determined that the nut or"stem" on the bottom of the valve was broken and was not allowing the <br /> valve to tighten and seat itself as designed. At 0903 the discharge to the SJR was stopped and the <br /> siphon box and CCC began to be drained. As the CCC and the siphon box were drained the leakage <br /> was observed by RWCF staff from around the top portion of the gate valve at an estimated rate of 20- <br /> gallons per minute (gpm). By 1500, the nut on the valve had been repaired and by 1530 treated <br /> wastewater was recirculating through the plant. At 1603 a Hazardous Material Spill Report was filed <br /> with the Office of Emergency Services and at 1610 the Regional Board was notified by telephone voice <br /> mail by Ms. Hinson of the leakage. At approximately 2000 hours on 7 December 2000, discharge to the <br /> SJR had resumed. <br /> Mr. Von Aspem pointed it out that on 5 December 2000,the Sr. Operator discovered that the siphon <br /> valve was opened only one-third of its capacity. If the valve is not opened fully then the elevation of <br /> treated wastewater in the CCC may rise to level above normal operating parameters. The siphon valve <br /> was fully opened after this discovery and the elevation head of the treated wastewater in the CCC <br /> returned to its standard operating height. This would mean that while the siphon valve was only <br /> partially opened, the treated wastewater in the CCC was at an elevation which was greater than that on <br /> the reverse side of the gate valve. Therefore, Mr. Von Aspem believes that the leaking was not <br /> occurring prior to 5 December 2000. <br /> Using the initial leakage rate of 20 gpm over a 41-hour period, it is possible that up to 49,200 gallons of <br /> non-disinfected wastewater may have leaked into the CCC. However, it is more realistic to consider the <br /> that the leaking only occurred during low tides, approximately one-third of the total time of the release <br /> or approximately 12 hours, which equates to 14,400 gallons. The incident report stated that the <br /> estimated leak rate was 2 gpm, considerably less than the estimate 20 gpm leak rate discussed during <br /> the time of my inspection. The incident report estimated that the lower leak rate might have occurred <br /> over a 41-hour period resulting in a release of up to 4,921 gallons. The recorded effluent discharge rate <br /> during the time of the release averaged approximately 29 million gallons per day. Using either <br /> approximation,the dilution of disinfected wastewater to the leaked non-disinfected wastewater is <br /> considerable. <br /> No receiving water specific sampling and analysis for total coliform organisms was conducted by the <br /> Discharger to determine the approximate extent of the release. However, the incident report indicates <br /> that analysis of a 24-hour composite sample collected from within the siphon box during the period in <br /> question, was well within the NPDES requirements. It is our understanding that the final effluent grab <br /> samples are collected within the CCC prior to dechlorination and not from within the siphon box. <br /> Mr. Von Aspem and the incident report indicate that a procedural change to the standard operating <br /> procedures has been made so that the non-disinfected wastewater will be continually drained to keep its <br /> elevation lower than that of wastewater within the CCC. This will effectively prevent any of the non- <br /> disinfected pond recirculation water from draining back into the CCC should the valve ever fail again. <br />
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