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ARCHIVED REPORTS_XR0006086
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3500 - Local Oversight Program
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PR0545603
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ARCHIVED REPORTS_XR0006086
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Last modified
9/29/2020 10:10:58 PM
Creation date
4/17/2020 1:57:35 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0006086
RECORD_ID
PR0545603
PE
3528
FACILITY_ID
FA0006095
FACILITY_NAME
PETERSON MFG
STREET_NUMBER
2403
STREET_NAME
NAVY
STREET_TYPE
DR
City
STOCKTON
Zip
95206
CURRENT_STATUS
02
SITE_LOCATION
2403 NAVY DR
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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SJGOV\sballwahn
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EHD - Public
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V � <br /> R <br /> • A S S O C I A T E S I N C <br /> In July 1994, a RESNA field geologist observed the drilling of four additional groundwater <br /> monitoring wells (MW4, MW5, MW6, and MW7) at the site to further characterize subsurface <br /> conditions Groundwater samples collected from these additional wells contained no detectable <br /> petroleum hydrocarbons A detailed discussion of the Phase II Subsurface Investigation can be <br /> found in RESNA's "Summary Report, July 1994 Investigation,"dated August 26, 1994 <br /> In PHS/EHD correspondence dated March 1995, regulatory approval was given to sample wells <br /> MW3 and MW5 and wells MW4, MW6 and MW7 on an alternating semi-annual basis MWI <br /> and MW2 were to be sampled every quarter, conditions permitting <br /> To further evaluate the extent of residual soil contamination in the vicinity of the former <br /> underground fuel storage tank (UST), Smith Technology supervised the advancement of four soil <br /> borings (SB-1, SB-2, SB-3, and SB-4) on February 29, 1996 to depths of approximately 16 to 26 <br /> feet bgs Total petroleum hydrocarbons as gasoline (TPHg), benzene, toluene, ethylbenzene, and <br /> xylenes (BTEX) were detected above method detection limits at low to moderate concentrations <br /> in samples collected at depths between 10 and 15 feet bgs in borings S13-1, SB-2, and SB-3 A <br /> detailed discussion of this subsurface investigation can be found in Smith Technology's <br /> "Subsurface Investigation Report, " dated April 30, 1996 <br /> GROUNDWATER MONITORING AND SAMPLING <br /> ATC personnel performed groundwater monitoring and sampling on May 16, 2001 Field work <br /> consisted of measuring the depth-to-water in wells MWI through MW7, using an electronic <br /> water/product interface probe to determine if free product was present, and purging and sampling <br /> wells MWI through MW7 <br /> Static groundwater elevations were measured in each monitoring well on May 16, 2001 <br /> Groundwater was measured at an average depth of approximately 1127 feet bgs A groundwater <br /> gradient map was created with the May 16, 2001 data The gradient map, presented as Figure 2, <br /> depicts a west to southwesterly groundwater gradient averaging 0 003 ft/ft or approximately 17 <br /> feet/mile The water table elevation has increased an average of 0 42 feet since the previous <br /> measurements were collected in August 2000 Groundwater monitoring data are summarized in <br /> Table 1 <br /> On May 16, 2001, groundwater samples were collected by ATC from monitoring wells MWI <br /> through MW7 Groundwater samples were collected from the monitoring wells after <br /> stabilization of pH, electrical conductivity (EC), and temperature All wells monitored were <br /> purged and sampled according to Smith Technology's Quality Assurance/Quality Control Plan <br /> on file with the PHS/EHD A minimum of approximately three casing volumes of water was <br /> removed from each sampled well A dedicated disposable bailer was used to collect each water <br /> • sample Field parameters and purged volumes are shown on well purge logs included in <br /> Attachment I <br /> 258031QUARTLYI2QR 2001 DOC 2 <br />
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