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ARCHIVED REPORTS_XR0007647
EnvironmentalHealth
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2900 - Site Mitigation Program
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PR0528359
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ARCHIVED REPORTS_XR0007647
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Last modified
5/8/2020 3:45:58 PM
Creation date
5/8/2020 3:19:43 PM
Metadata
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Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0007647
RECORD_ID
PR0528359
PE
2950
FACILITY_ID
FA0019146
FACILITY_NAME
SHELL OIL PRODUCTS US
STREET_NUMBER
3725
Direction
N
STREET_NAME
TRACY
STREET_TYPE
BLVD
City
TRACY
Zip
95304
APN
21217030
CURRENT_STATUS
02
SITE_LOCATION
3725 N TRACY BLVD
P_LOCATION
03
P_DISTRICT
005
QC Status
Approved
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EHD - Public
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C A M B R I A <br /> concentration in monitoring well MW-1A versus time Cumulative mass removed is also shown <br /> on the graph <br /> ANTICIPATED FIRST QUARTER 2003 ACTIVITIES <br /> Groundwater Monttoring. Blaine will gauge and sample the site wells according to the existing <br /> sampling schedule and tabulate the data Cambria will prepare a groundwater monitoring report <br /> Groundwater Remediation OWE from well MW-IA will continue and will resume from <br /> well BF-1 <br /> Onsite Abandoned Water Well Cambria will submit a work plan for the destruction of the <br /> abandoned water well at this site We will also submit an application for a permit to destroy the <br /> well, along with the permit fee Currently the well destruction activities are scheduled for <br /> February 13 and 14,2003 <br /> CONCLUSIONS AND RECOMMENDATIONS <br /> Well MW-IA contained MTBE at a concentration of 470 gg/L, which remains significantly <br /> reduced from MTBE concentrations reported in the first quarter of 2002 It appears that periodic <br /> GYVE continues to reduce MTBE concentrations in well MW-1A Groundwater flow direction <br /> was to the northeast this quarter, as is typical for the site <br /> CLOSING <br /> If you have any questions regarding the contents of this document, please call Joe Neely at <br /> (707) 933-2361 <br /> 0813 2 <br />
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