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ARCHIVED REPORTS_XR0010320
EnvironmentalHealth
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EHD Program Facility Records by Street Name
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S
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SONORA
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3500 - Local Oversight Program
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PR0545695
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ARCHIVED REPORTS_XR0010320
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Last modified
5/27/2020 5:19:46 PM
Creation date
5/27/2020 4:52:25 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0010320
RECORD_ID
PR0545695
PE
3528
FACILITY_ID
FA0003877
FACILITY_NAME
CITY OF STOCKTON FIRE STATION #2
STREET_NUMBER
110
Direction
W
STREET_NAME
SONORA
STREET_TYPE
ST
City
STOCKTON
Zip
95203
APN
13731025
CURRENT_STATUS
02
SITE_LOCATION
110 W SONORA ST
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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EHD - Public
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1 <br /> t25 February 2005 <br /> S AGE-NC Project No 01-0827 <br />' Page 2 of 10 <br />' repair pit located at the western edge of the building <br /> In October 1992 UST#2, UST#3 and UST#5 were removed from the site, along with the dispenser <br /> lines which served the site's dispenser located at the southwestern corner of the building UST#5 was <br /> a 500 gallon UST used for the storage diesel fuel UST#2 was a 1,000 gallon gasoline UST and <br /> UST#3 was a 500 gallon diesel UST These two USTs serviced the western dispenser on the on the <br />' fuel island Contamination was reportedly evident on the southern excavation wall However,the <br /> only sample with reported hydrocarbons was collected at the dispenser island (P1) Sample P-1 <br /> contained at total petroleum hydrocarbons as gasoline (TPH-g), and TPH-diesel (TPH-d) and <br />' toluene, ethyl-benzene and xylene at concentrations of 1,600 mg/kg, 4,900 mg/kg, 0 33 mg/kg, <br /> 4 9 mg/kg and 56 mg/kg, respectively Analytical results of soil samples are depicted in Table 1 <br />' 22 SITE ASSESSMENT MILESTONES <br />' In December 1988 the assessment of the petroleum hydrocarbons release from the USTs began with <br /> the installation of soil borings B 1 through B3,completed as ground water monitoring wells MW-1 <br /> • through MW-3 Soil samples from boring B 1 contained TPH-g at a maximum concentration of <br /> 350 mg/kg (111-25) BTEX was detected in the same sample at concentration of 4 7 mg/kg, <br /> 21 mg/kg, 18 mg/kg and 110 mg/kg,respectively Analytical results of soil samples are depicted in <br /> Table 1 <br /> Monitoring well MW-1 was installed at the western edge of the former UST cluster area,well MW-2 <br /> was installed 100 feet east of well MW-1 and well MW-3 was installed 90 feet south of well MW-1 <br /> and the former UST excavation The wells were first sampled on 12 December 1988 <br /> In May 1990,five additional soil borings,B4 though B8 were established on the site Boring B8 was <br /> completed as monitoring well MW-4,at a location 140 feet north of well MW-1 and the former UST <br /> excavation <br /> In August and September 1992,five additional soil borings,B9 though B 13,were established on the <br /> site Boring B 13 was completed as remediation well RW-1,at a location 20 feet north of well MW-1 <br /> I and the former UST excavation Boring B 12 was completed as ground water observation well PZ-1 <br /> between well RW-1 and the former UST excavation Additionally, boring B9 was completed as <br /> vapor well VW-1, boring B 10 was completed as vapor well VW-2 and boring B 11 was completed <br /> as duel-screened vapor well VW-2 During September 1992 a set of ground water and soil vapor <br /> extraction(SVE)remediation feasibility pilot studies were conducted on the site One ground water <br /> extraction(GWE)pilot test was conducted at well RW-1 and one SVE pilot test were conducted on <br /> wells VW2 and VW-3 <br /> IAdvanced GeoEnvironmentai,Inc <br />
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