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COMPLETION OF MONITOR WELL MW4 <br /> Monitor well MW4 was completed with 10 feet of machine slotted SCH 40 TriLock 2 <br /> inch diameter PVC screen (0 020) from 70 feet bgs to the total depth of the well at SO <br /> feet bgs The well was completed to surface with blank SCH 40 TriLock 2" diameter <br /> PVC The sand envelope consisted of 93 Monterey sand and was positioned from the <br /> base of the well to two feet above the top of the slotted casing The sand envelope was <br /> sealed on top with a 2 5-foot layer of hydrated bentonite pellets Cement (with less than <br /> 5% bentonite) was used to seal the annular space from the top of the bentonite seal to <br /> surface A locking thermos cap was used to seal the casing orifice A steel traffic box <br /> fitted with a locking system was set in concrete to protect the exposed well casing <br /> A construction diagram of the monitor well is included in Appendix D of this report <br /> DEVELOPMENT AND SURVEYING OF MONITOR WELL MW4 <br /> WEGE and Pittman Well Purging developed the new monitoi well on June 20, 2001 A <br /> two inch diameter-swabbing tool was used to agitate and condense the sand pack across <br /> the slotted casing intervals The wells were then purged with a truck mounted vacuum <br /> lift pump until solids were removed from the well casing and the ground water entering <br /> through the sand pack was no longer turbid Approlimately 50 gallons of water were <br /> purged from the 2-inch diameter well <br /> A licensed surveyor from Kjeldsen, Sinnock, and Neudeck, Inc suiveyed the elevation of <br /> top of the new well casing with respect to an existing benchmark on June 25 2001 The <br /> surveyor also resurveyed the elevations of the existing 3 monitor wells and provided <br /> i ectangular coordinates for all four wells The locations of the wells are shown in Figure <br /> 3 The elevations of the casing tops are included in Table 2 <br /> The re-survey of the existing monitor wells MW I, MW2, and MW3 showed them to be <br /> 0 66-0 67 feet lower in elevation than previously reported All three wells however, <br /> showed the same elevation decrease of 0 66 to 0 67 feet, indicating a change in the survey <br /> reference point rather than the monitoring wells The change in groundwater elevations <br /> at the wells, therefore, had no effect on past determinations of groundwater flow <br /> directions and gradients at the site <br /> COLLECTION AND ANALYSIS OF GROUNDWATER SAMPLES FROM l NN/4 <br /> A WEGE geologist collected groundwater samples from monitor well MW4 on July 25, <br /> 2001 Prior to sampling the well was purged of approximately 50 gallons of water using a <br /> Grundfoss submersible pump and dedicated poly tubing <br /> After purging, the well was allowed to recover to at least 80% of its original well volume <br /> A groundwater sample was then collected with a disposable polyethylene bailer and <br /> decanted with no head space into two 40 ml VOA vials containing 0 5 ml HCL acid as a <br /> preservative <br /> 5 Arc Pump QM 4-6, 2001 <br />