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ARCHIVED REPORTS_XR0007240
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3500 - Local Oversight Program
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PR0540315
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ARCHIVED REPORTS_XR0007240
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Last modified
7/7/2020 3:03:06 PM
Creation date
7/7/2020 2:46:30 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0007240
RECORD_ID
PR0540315
PE
3526
FACILITY_ID
FA0023046
FACILITY_NAME
U-HAUL FACILITY NO 710050
STREET_NUMBER
2701
Direction
N
STREET_NAME
WILSON
STREET_TYPE
WAY
City
STOCKTON
Zip
95215
APN
11708014
CURRENT_STATUS
01
SITE_LOCATION
2701 N WILSON WAY
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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EHD - Public
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' I I In,I# QYi 50 131-10, Ill\11011111(ili It <br /> Ri nu cIi i1 Fe,istbdil` I,,i Rep)i i I CbI It 111 2 , 1200, <br /> ' concentrations of approximately 4%, 3 5%, and 2%, respectively This response was likely due to the <br /> infection of sparge air The remaining three monitonng point wells (MW-1C, MW-2C, MW-9B) did not <br /> ' display significant variation of dissolved oxygen concentrations <br /> tLaboratory analysis of groundwater samples collected from monitor well MW-3B before and after the <br /> AS test indicated a significant change in dissolved hydrocarbon concentrations Analytical results <br /> ' indicated that volatile fuel hydrocarbon concentrations in MW-3B increased from 640,000 micrograms <br /> per liter (ug/1) prior to AS testing, to 12,000,000 ug/1 immediately following the conclusion of AS <br /> testing The increase in volatile fuel hydrocarbons may be attributed to adsorbed hydrocarbons being <br /> mobilized into groundwater Additionally,BTEX concentrations in groundwater collected from MW-3B <br /> ' decreased following AS testing The decrease in BTEX concentrations may be attnbuted to the air <br /> stripping (converting to vapor phase) as a direct result of the AS remediation The groundwater samples <br /> ' collected from MW-3C did not display any significant variation of dissolved-phase hydrocarbon <br /> concentrations before and after the AS test Laboratory analytical results of groundwater samples <br /> • collected for the AS test are presented in Table 5 A copy of the laboratory analytical report is provided <br /> in Appendix F <br /> ' 4 1 4 Air Sparge Test Results <br /> ' Based on AS testing data, groundwater analytical results, and field observations, the effective AS ROI <br /> (intuitive estimation between induced pressure response and dissolved oxygen increases versus distance <br /> ' in the monitoring point wells) approaches an estimated 20 foot radial distance from test well ASW-1 <br /> The ASW-1 test data was plotted on a well performance curve (pressure versus flow rate) and is <br /> presented as Figure 3 The estimated AS ROI for the site is presented in Figure 4 Based on the AS test <br /> tresults, a remedial system incorporating groundwater AS would likely be an effective treatment <br /> technology for the remediation of groundwater beneath the site <br /> 4 2 VAPOR EXTRACTION TESTING <br /> ' VE testing was conducted at the site on November 19, 2002 in order to determine the feasibility of <br /> utilizing VE to remediate petroleum hydrocarbon impacted soil beneath the site The VE test equipment <br /> was transported to the site and initially manifolded to remedial well VEW-1 and subsequently to <br /> ' 10 <br />
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