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COMPLIANCE INFO_2016 - 2018
Environmental Health - Public
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COMPLIANCE INFO_2016 - 2018
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Last modified
12/8/2023 12:57:00 PM
Creation date
11/5/2018 4:45:56 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2300 - Underground Storage Tank Program
File Section
COMPLIANCE INFO
FileName_PostFix
2016 - 2018
RECORD_ID
PR0505867
PE
2361
FACILITY_ID
FA0007059
STREET_NUMBER
192
STREET_NAME
LATHROP
STREET_TYPE
Rd
City
Lathrop
Zip
95330
CURRENT_STATUS
01
SITE_LOCATION
192 Lathrop Rd
P_LOCATION
07
P_DISTRICT
003
QC Status
Approved
Scanner
SJGOV\rtan
Supplemental fields
FilePath
\MIGRATIONS\L\LATHROP\192\PR0505867\COMPLIANCE INFO 2016 - JUNE 2017.PDF
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EHD - Public
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MONITOFWG SYSTEM CERTIFI*TION <br />CERTIFICATION /TEST DATE: January4, 2017 <br />Al. FACILITY <br />Name Colonial Energy #40135 <br />Address 192 Lathrop Road, Lathrop, CA 95330 <br />Phone# 209-858-4998 <br />Contact Station Manager <br />A2. OWNER <br />Name Colonial Energy, LLC. <br />Address 2860 N. Santiago Blvd. 2nd Floor, Orange, CA 92867 <br />Phone# 714-761-5426 <br />Contact Victor Hassan <br />D. RESULTS OF TESTING / SERVICING <br />Make / Model of Monitoring System: Veeder-Root TLS -350 SN# 80548678305001 <br />Software Version Installed: 327.04 <br />Complete the following checklist: <br />■ Yes <br />Is the audible alarm operational? - - <br />❑ No <br />■ Yes <br />❑ No' <br />Is the visual alarm operational? - <br />■ Yes <br />❑ No " <br />Were all sensors visually inspected, functionally tested, and confirmed operational? <br />■ Yes <br />❑ No " <br />Were all sensors installed at lowest point of secondary containment and positioned so that other equipment <br />will not Interfere with their proper operation? <br />❑ Yes <br />❑ No " <br />■ NIA <br />If alarms are relayed to a remote monitoring station, is all communications equipment (e.g. modems) <br />operational? - <br />■ Yes <br />■ Yes <br />❑ No' <br />NIA <br />❑ No' <br />For pressurized piping systems, does the turbine automatically shut down if the piping secondary containment <br />monitoring system detects a leak fails to operate, or Is electrically disconnected? If yes: which sensors initiate <br />positive shutdown? (check all that apply) ■ SumpRrench sensors; ■Dispenser Containment Sensors. <br />Did you confirm positive shut -down due to leaks and sensor failureldisconnection? <br />❑ Yes <br />❑ No* <br />■ NIA <br />For tank systems that utilize the monitoring system as the primary tank overfill warning device (i.e. no <br />mechanical overfill prevention valve is installed), is the overfill warning alarm visible and audible at the tank <br />fill point(s) and operating properly? If so, at what percent of tank capacity does the alarm trigger? _ e/ <br />■ Yes' <br />❑ No <br />Was any monitoring equipment replaced? If yes, identify specific sensors, probes, or other equipment replaced <br />and list the manufacturer name and model for all replacement parts in Section E, below. <br />■ Yes' <br />❑ No <br />Was any liquid found inside any secondary containment systems designed as dry systems? <br />(Check all that apply) ❑ Product; ■ Water. If yes, describe causes in Section E, below. <br />■ Yes ❑ No " Was monitoring system set-up reviewed to insure proper settings? Attach set-up reports, If applicable. <br />■ Yes ❑ No' Is all monitoring equipment operational per manufacturer's specifications? <br />" In Section E below, describe how and when these deficiencies were or will be corrected. <br />E. COMMENTS <br />Removed a small amount of rainwater from all stp sumps. <br />Replaced all tank annular sensors with 794390-460 sensor. Orignal (0794390-420) were too short, and sensor was not reaching <br />annular space bottom. <br />is 2017 Walton Engineering, Inc. <br />Page 2 of 3 <br />
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