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California Regional Water Quality Control Board <br /> Central Valley Region <br /> �iH Hickox Robert Schneider,Chair <br /> etary for Gray Davis <br /> vrronme 0 Sacramento Main Office Governor <br /> Protection Internet Address http//www swrcb ca gov/rwgcb5 <br /> 3443 Routier Road,Suite A,Sacramento,California 95827-3003 <br /> Phone(916)255 3000-FAX(916)255-3015 <br /> 13 March 2002 - ' 11-74 <br /> Mr Bob Cochran Ivern and Roger Baffoni MAR 15 2001 <br /> Chevron Products Co 1175 Orangewood Dave b y�-------- _...._-____- <br /> PO Box 6004 Lodi, CA 95240 <br /> San Ramon,CA 94583 <br /> REVIEW FOURTH QUARTER 2001 PROGRESS REPORT AND FINAL REMEDIA TION PLAN <br /> ADDENDUM, FORMER CHEVRONSTATION#9-5775, 301 WESTKETTLEMANLANE,LODI, <br /> CLEANUP AND ABATEMENT(C&A) ORDER NO 5-00-704 <br /> Board staff reviewed the 1 i January 2002 Quarterly Progress Report, Fourth Quarter 2001 (Q4-2001 Report) <br /> and the 9 January 2002 Final Remediation Plan Addendum (FRP Addendum)both submitted by Secor <br /> International Incorporated(Secor) for the subject site The Q4-2001 Report documents decreasing trends of <br /> petroleum hydrocarbon and MtBE constituents in on-site monitoring and extraction wells due to continued <br /> remedial activities at the site The FRP Addendum includes a proposal to defer off-site groundwater extraction <br /> as previously proposed by Secor in June 2001 and approved by this office in July 2001 <br /> Concentrations of petroleum hydrocarbons and MtBE have decreased significantly since the soil vapor <br /> extraction(SVE) and groundwater extraction and treatment(GET) systems began operation in July 2000 As of <br /> December 2001,4 4 million gallons of contaminated groundwater from the former Chevron site has been <br /> extracted,treated with carbon, and discharged to the City of Lodi industrial sewer line MtBE has decreased in <br /> on-site monitoring wells, and the GET system influent concentration has stabilized at approximately <br /> 130 micrograms per liter(µg/1) <br /> In combination, the SVE and GET remedial systems Have reportedly removed 671 gallons of total petroleum <br /> hydrocarbons as gasoline(TPHg), 12 gallons of benzene, and 85 gallons of MtBE The continued groundwater <br /> extraction appears to be effectively stabilizing the on-site groundwater plume, and reducing groundwater <br /> contaminants Currently, only one off-site well (MW-9) shows a detection of MtBE at 10 (µg/1) During the <br /> Q4-2001 sampling event,MtBE was only detected in A-zone(45 to 66 feet) monitoring wells, and was not <br /> detected in monitoring wells completed in the B (76 to 90 feet) or C (105 to 112 feet)aquifer zones <br /> Concentrations of MtBE in extraction well EX-1 have decreased from a maximum of 720,000 µg/1 in March 2000 <br /> to 13,000 µg/l m November 2001 The 13,000 µg/1 in extraction well EX-1 is currently the highest MtBE <br /> concentration at this site <br /> Based on declining concentrations of groundwater contaminants both on-site and off-site, Secor proposes not to <br /> install and operate groundwater extraction wells on the property south of Kettleinan lane as proposed in Secor's <br /> June 2001 addendum to the Final Remediation Plan Board staff met with Bob Cochran from Chevron and <br /> Secor personnel on 13 November 2001 to discuss these changes, and Board staff agreed that groundwater <br /> California Environmental Protection Agency <br /> g cY <br /> CoRecycled Paper <br /> The energy challenge facing California is real Every Californtan needs to take arumcdiate action to reduce energy consumption <br /> For a list of simple ways you can reduce demand and cut your energy costs,see our Web-site at http l/www swrcb ca govhwgcb5 <br />