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' la wal Tte/rnfU 199 Pae 11 <br /> Gea g � <br /> Dual Phase Extraction Pilot Test Report <br /> Project No 723 2 <br /> November 12,2004 <br /> ' oxidants) while a negative value indicates a reducing environment APT staff monitored <br /> these parameters while the wells were sampled prior to injection during each event In the <br /> APT report's Figure 1 it can be seen that the ORP values rose right after the first injection <br /> event in wells MW-9 and GP-1 Conversely, well GP-2 exhibited a slow increase until a <br /> sharp decline in ORP on June 11 The differences in the wells' ORP response suggests that <br /> ' the fast response in GP-1 was due to the fracture/lithologic pathway discussed above while rr <br /> the response in GP-2 was more reflective of slow diffusion of th'einjectio en fects But the <br /> theory that a sand/silt layer exists that intersects both MW-9 and GP-1 wells screens but not <br /> ' the screen of GP-2 is not realistic given the short lateral distance separating the wells (24") <br /> Therefore, the fast response in GP-1 is probably a result of a drilling artifact fracture rather <br /> than a sand/silt preferential pathway <br /> ' The ORP values from GP-3 fluctuated without a trend for the first six events and then <br /> declined strongly on and after June 11 This suggests that the oxidant injection did not <br /> influence this well and the pilot test's definitive radius of influence was less than 48 inches <br /> from well MW-9 The TPH-G increases/ORP declines recorded at the end of the pilot test <br /> ' may have been the result of the injection pressures applied to the subsurface causing <br /> mobilization of contamination previously trapped in pore spaces <br /> 6.0 DISCUSSION <br /> ' The test demonstrated that oxidants can destroy the contamination in groundwater at the site <br /> but the radius of influence is limited due to the clayey soils at the site There were limitations <br /> in the test that should be taken into account regarding the radius of influence demonstration <br /> The length of the well screen in MW-9, 15 -- 35 feet bgs, was excessive as compared <br /> to air sparging wells which are typically constructed with screens less than 5 feet in <br /> ' lengtho p <br /> The depth of the well screen in MW-9, 15 — 35 feet bgs, exceeded the bottom of the <br /> GeoprobeTM well monitoring points screened at 20 - 30 feet bgs. It is possible that if <br /> ' a sand/silt preferential pathway existed below 30 feet bgs then the infected oxidants <br /> could have bypassed the monitoring points <br /> a Due to the tight formation it is possible that some of the infected oxidants may have �o A <br /> ' exited the top of the MW-9 well screen above the water table and the contaminant <br /> decay was weighted toward vadose zone sediments <br /> ' • The total volume of H202 solution injected was a fraction of the pore space within the <br /> monitored area In their report APT states that the amount of solution injected was <br /> less than 2% of the volume of water in a four foot radius centered on MW-9 If we <br /> ' assume the treated area is a cylinder centered on well MW-9 with a height of 20 feet <br /> (screened interval), a radius of four feet and a porosity of 50% (clay) this represents <br /> approximately 3,762 gallons* The total amount of solution infected was 15 gallons <br />