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3rd Quarter Report - Beacon Station #695 3 December 1992 <br /> Although vapor concentrations generally declined at the individual <br /> extraction points during the 3rd quarter, concentrations remained above <br /> several thousand parts per million (ppm) at many locations. This <br /> suggested that a significant residual contaminant mass was still present <br /> at the conclusion of the quarter. <br /> During the 3rd quarter the ongoing remedial program eclipsed the 50,000 <br /> pounds extracted mark, indicating that significant progress has been made <br /> in evicting the contaminant mass from the subsurface. Over 16,000 pounds <br /> of hydrocarbons were extracted during the 3rd quarter alone. <br /> Efforts were made to increase the extraction flowrate from the ground by <br /> completely closing ambient dilution and by eliminating one of two <br /> undersized, restrictive piping connections between the systems three <br /> manifold boxes and the vacuum pump. <br /> On 22 September, the final date of monitoring during this quarter, the <br /> efforts to improve system performance had been successful in increasing <br /> the hydrocarbon extraction rate to 263 pounds per days (lbs/day) . <br /> II . RECOMMENDATIONS <br /> To further increase the flowrate from the soils, the second restrictive <br /> connection between manifold boxes should be eliminated as soon as <br /> possible. If further improvements are still desired, other options <br /> include repulleying the pump or replacing the vacuum pump drive motor <br /> with a higher rated unit <br /> Given the level of residual hydrocarbons observed at the conclusion of <br /> the third quarter, it is likely that the current program utilizing the <br /> catalytic incinerator will need to be continued at least through the end <br /> of the 4th quarter. <br /> III. INDIVIDUAL MONITORING EVENTS <br /> The following section describes how the system was adjusted during each <br /> monitoring within the performance limits of the equipment and the <br /> compliance limits of the operating permit issued for the system <br /> 1 July 1992 Monitoring: <br /> The SUES was apparently shut down on 18 June while routine groundwater <br /> monitoring activities were being undertaken. The system was restarted on <br /> 30 June and allowed to purge a full day prior to monitoring on 1 July. <br /> On 1 July, vapor concentrations remained quite high at many extraction <br /> points with a region of 10,000+ ppm concentrations present between the <br /> gasoline and diesel pump islands. Side by side wells MW-3 and MW-10, <br /> which appeared to be near the heart of the plume, both had 10,000+ ppm <br /> concentrations suggesting that high levels of soil gases were present in <br /> -2- <br />