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SENT BY:9163622318-Sacra. , CA ; 4-17- 0 ; 1:32PM ;RADIAN INTERNATIONAL 2094683433;# 2/ 9 <br /> DDJC-Tracy EW005 Abandonment Work Plan <br /> 1.0 INTRODUCTION feet.There is a 5-foot collar with blank casing <br /> 40 to 45 feet from the base of the vault.The <br /> The purpose of this work plan is to surnmarize total depth of the borehole drilled for the well <br /> the activities necessary to perform the gs. Attachment 1 to this work plan <br /> abandonment of extraction well(EW)005AU, truction log for EW005AU. <br /> located along the northern boundary of the - <br /> Defense Distribution San Joaquin(DDJC)Tracy 1.2 1999 EW005 Inspection <br /> Site(Figure 1-1;Note:The location of <br /> EW005AUA is shown on the figure;this well 1.2.1 On 12 October 1999,representatives <br /> replaced EW005AU,and was installed from Radian and Gregg Drilling visited the site <br /> approximately 10 feet from the original well). to determine the best approach to abandon the <br /> The work performed will be conducted in well. During this visit,the well was sounded <br /> accordance with the general procedures, with a weighted tape to determine the actual <br /> specifications,and requirements set forth in the depth of the well.The attempt to reach the <br /> Comprehensive Field Work Plan—Volume I of bottom of the well was unsuccessful, with the <br /> 2-SharpelTracy Sites, California(Radian treasuring tape stopping at a depth of <br /> International, 1998a).Also included in this approximately 37 feet bgs, <br /> EW003AU abandonment work plan is a <br /> summary of a previous abandonment attempt,a 1.2.2 During the 12 October visit to the site, <br /> recent inspection,and an attempted video survey several items that raise logistical concerns were <br /> of EWOO5AU.Currently planned abandonment noted.Overhead utilities are located directly <br /> activities are discussed in Section 2.0.These above the former extraction well.The well is <br /> include pump removal and well abandonment by also located adjacent to the concrete drainage <br /> pressure grouting;if pump removal is not canal that runs along the northern boundary of <br /> possible,abandonment will be accomplished by the DDJC-Tracy facility.The canal wall is <br /> overdrilling and grouting.Both of these approximately 4 inches away from the well <br /> abandonment options are described below. casing,making it difficult to overdrill the well <br /> without causing damage to the concrete.It will <br /> 1.1 1998 EW005 Abandonment be necessary to place steel plating over the canal <br /> Attempt to allow drill rig access.The well cannot be <br /> accessed for overdrilling unless the security <br /> 1.1.1 Abandonment of EW005AU was . fence along the north boundary of the depot <br /> attempted by Radian International (Radian)and property is temporarily removed during the <br /> Gregg Drilling in April of 1998,During the abandonment effort. <br /> abandonment effort,an unsuccessful attempt <br /> was made to remove the pump from the well.It 1.3 1999 EW005 Video Survey <br /> was concluded that there may have been well Attempt <br /> casing collapse because the pump could not be <br /> retrieved.A summary of these activities is 1.3.1 A downhole video survey of EW00SAIJ <br /> documented in a Radian memorandum dated 1 was attempted on 18 November 1999 to <br /> May 1998 (Radian international, 1998b). determine the position of the pump in the well <br /> and the condition of the well casing.The video <br /> 1.1.2 Review of well construction records for survey,however,was unsuccessful because the <br /> EW005 indicated the well was located in a 4- camera would not fit in the well with the pump <br /> foot by 4-fool vault,constructed below ground and drop pipe.A camera of smaller diameter <br /> surface. Well construction consisted of a 6-inch that could be inserted into the well for the video <br /> diameter PVC-cased well to a depth of 20 feet survey was not available.Therefore,no video <br /> below ground surface(bgs).A 6-inch diameter survey was completed. <br /> stainless steel screen is in place from 20 to 40 <br /> 131W005_AbMdWmmt l December 1999 <br />