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ARCHIVED REPORTS XR0006465
Environmental Health - Public
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2900 - Site Mitigation Program
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PR0519189
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ARCHIVED REPORTS XR0006465
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Last modified
8/21/2019 4:52:07 PM
Creation date
8/21/2019 2:51:38 PM
Metadata
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EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0006465
RECORD_ID
PR0519189
PE
2950
FACILITY_ID
FA0014347
FACILITY_NAME
CURRENTLY VACANT
STREET_NUMBER
6425
STREET_NAME
PACIFIC
STREET_TYPE
AVE
City
STOCKTON
Zip
95207
APN
09741031
CURRENT_STATUS
02
SITE_LOCATION
6425 PACIFIC AVE
P_LOCATION
01
QC Status
Approved
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to be a reading of 500 on the PID. On January 14 , 1991 , the PID <br /> registered 250 , and a slight odor was noted from the exhaust of <br /> the charcoal. A bag sample was then obtained and brought back to <br /> Western Geo-Engineers portable laboratory in Woodland, California, <br /> late in the evening. The sample was immediately run the next <br /> morning and determined that breakthrough had occurred. The pilot <br /> test was then terminated that day, see Tables 1 , 2 , and 3. During <br /> the source test, bag samples were obtained from monitor well MW10 <br /> and showed a relatively stable vapor stream consisting of 119 to <br /> 164 mg/L (31 ,000-42,700 ppm gasoline vapor) of Total Fuel <br /> Hydrocarbons (TFH) in air along with 14% methane (Stockton area is <br /> a known basin for natural gas production and it is believed that <br /> this methane is produced from the underlying formations and not <br /> from a leak in the gas main) . At the completion of the test the <br /> extraction system was connected to the excavation wells so <br /> samples could be obtained from that source area. Steady state was <br /> probably not reached in the excavation during the short half hour <br /> duration of vapors being pulled from that area, but sample <br /> analyses indicates a similar vapor stream of 32,800 ppm TFH and <br /> 14% methane. All bag (tedlar) samples were analyzed for Total <br /> Fuel Hydrocarbons (TFH) as gasoline along with Benzene, Toluene, <br /> Ethylbenzene and Xylenes (BTEX) using DHS headspace method with <br /> FID chromatograph Western Geo-Engineers (WEGE) . Also a methane <br /> analysis was run using a dedicated methane infrared analyzer with <br /> the FID chromatograph for confirmation. An influent sample to the <br /> charcoal was obtained prior to shutting the system off and <br /> disconnecting it from the wells (for analysis by Chemtech <br /> • Laboratories ) . This sample was analyzed using EPA modified 8015 <br /> and 602 for TPH and BTEX, respectively, and used to profile the <br /> charcoal drums for shipment for regeneration. Throughout the <br /> test, vacuum readings were obtained from the ground water <br /> monitoring wells, to help establish the radius of influence of the <br /> vapor extraction system, see Figure 6B. <br /> This source test will help evaluate the amount of fuel range <br /> hydrocarbons available and the supplemental fuel/oxygen needed to <br /> achieve incineration using the Hirtz Incenerator for emissions <br /> control during ground water and soil remediation for this site, <br /> see Figures 7 manifold for vapor extraction system and 8 schematic <br /> for vapor extraction system. <br /> If you have any questions, please call (916) 662-4541 . <br /> i <br /> Sincerely yours, <br /> George' L. Converse <br /> • Project Geologist <br /> cc: Mr. Dick Cunningham, R. J. Cunningham and Assoc. <br />
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