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R603 UPDATE-21 10/15/93 <br /> V <br /> ULTS � <br /> APOR RECOVERY_OPERATIONS AND RES <br /> Presently (September 29, 1993) the REMOX units have operated for <br /> a total of 10767 hours out of a total of 16581 hours (65%5) . The <br /> new replacement unit has operated 6765 hours out of 9934 hours <br /> (68%) , removing and destroying and estimated 70752 pounds of <br /> gasoline range hydrocarbons and an estimated 65487 pounds of <br /> oxidized gasoline range hydrocarbons as CO2 (September 29, 1993) <br /> for a total of 136239 pounds or 21798 gallons of gasoline range <br /> hydrocarbons removed from the subsurface, see Tables 2, and 3 and <br /> Appendix C-Air Monitoring Report . <br /> Since February 18, 1993 the vapor recovery/destruction has been <br /> declining from an average above 200 pounds per day of gasoline <br /> range hydrocarbons to a low of 30 pounds per day of gasoline <br /> range hydrocarbons on July 19, 1993 With the addition of the <br /> heat exchanger the pounds per day destruction was increased to <br /> nearly 70 pounds per day on August 23 , 1993 , dust prior to <br /> turning the system off for repair of the compressor, see Table 2 <br /> and concentration charts Figures 5A, 5B and 5C. These charts <br /> indicate that the heavier compounds of gasoline range <br /> hydrocarbons ethylbenzene, xylenes, etc. ) have been moderately <br /> reduced while lighter compounds (benzene, toluene, etc ) have <br /> been greatly reduced <br /> CONDENSATE REMOVAL BY LTT <br /> Condensation from vapor extraction is collected in moisture drop <br /> out tanks constructed of 12" PVC pipe, before the manifold, to <br /> prevent moisture build up on the vacuum pump filter. All fluids <br /> removed from the condensation traps are placed in the 1000 gallon <br /> "ConVault" Table 5 represents the field notes from LTT <br /> condensate/water removal, see Appendix B As of August 30, 1993 <br /> LTT has removed an estimated 4915 gallons of condensate/water and <br /> 26 . 25 gallons of product from the condensate traps . Total fluids <br /> removed as of August 30 , 1993 : 5077 gallons of water/condensate <br /> and 48 75 gallons of product (162 previously recovered condensate <br /> water and 22 5 gallons of product) . <br /> 4 . 0 SUMMARY <br /> There has been no evidence of floating product or product sheen <br /> on the ground water in MW1 since April 14, 1992 and MW3 and MW10 <br /> since November 11, 1992 . Only occasional product sheen is found <br /> with the condensate recovered from the vapor extraction moisture <br /> dropouts and manifold. Vapor recovery and well purging has <br /> reduced the hydrocarbons in ground water significantly since the <br /> May 25, 1990 sampling, see Table 1 . Using benzene as an <br /> indicator, monitoring wells MW4, MW5, MW6, MW7 and MW9 have been <br /> reduced to below detection limits while the wells being utilized <br /> for vapor extraction (MW1, MW3 , and MW10) have been reduced by <br /> better than 99% . MW2, which is also utilized for vapor <br /> extraction has been reduced 81% and MW8 has been reduced by <br /> PAGE 3 <br />