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PAGE 2 <br /> HISTORY OF OIL b GAS WELL <br /> 11/ 3/79 Wipe hole 10 stands at 4590 ' . <br /> Survey and tripped for new bit at 4735 ' <br /> Wiped hole 10 stands at 5145 ' <br /> 11/ 4/79 Survey and tripped for new bit at 5 , 540 ' . <br /> Drilled 7-7/8" hole to total depth.. 5 ,820 ' . ;lade 20 stand wiper <br /> run, circulated hole clean, and pulled out or hole . Rigged up <br /> Schlumberger and started running logs at 7 : 00 p.m. <br /> Ran Combination Dual Induction - SFL and Sonic log from 800 ' to <br /> ..... ........ <br /> 5803' . _.. ........ <br /> Continuous dipmeter. <br /> From 3500' to 58091 . <br /> Release Stratigraphic mud logging unit at midnight . <br /> 11/ 5/ 79 Finished running Schlumberger lobs and prepared to plug and <br /> abandoned well . Plugged well as follows : <br /> 1. Plug #1 (shoe) hung drill, pipe at $.4..6 ' , B-J mixed , pumped , <br /> and equalized 60 sacks of Class "G" treated with 3% CaCl2 . <br /> Calculated to fill 200 ' . CIP at 8: 55 a.m. . Wait on cement <br /> 3 hrs and local!014 top of cement at 790 ' . Re-cemented , hung <br /> drill pipe at .I44' and equalized 30 sacks of Class "G" with 3% <br /> CaC12. Calculated to fill to 695 ' . Cement in place at 11. : 50 <br /> a.m. . Plug approved by Jim Champion - DOG Engineer . <br /> 2. Plug #2 (fresh water) hung drill pipe at 249ā€ž' and equalized 30 <br /> sacks Class "Gā€ treated with 32 CaCl2 . Calculated fill to 1.53 ' . <br /> C. I . P . at 1 : 55 p.m. . Plug..ap_p.poved . by Jim Champion-DOG Engineer . <br /> 3. Plug Top of Surface Casing. Hung drill pipe at ,, .(!" and equalized <br /> 10 sacks of Class "G" cement treated with 3% CaC12. Plug approved <br /> by Jim Champion DOG Engineer. Cut off casing at collar floor and <br /> weld on steel plate. <br /> Laid down kelley , rat hole , mouse hole , tear out BOP . Clean mud <br /> tanks rig released 'at 10:00 p.m. 11/5/79 . <br />