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detected in soil samples submitted for laboratory analyses from SB3. Site activities are <br /> summarized in ATC's Summary Report for Subsurface Investigation, dated October 20, 1997, <br /> From September 25 to 28, 1998, ATC personnel supervised the advancement of soil boring to a <br /> depth of approximately 65 feet bgs. This boring was completed as groundwater monitoring well <br /> MW1. Analytical data indicated that -soil and groundwater samples contained detectable <br /> concentrations of petroleum hydrocarbons. Field activities and analytical-results are detailed in <br /> ATC's Summary Report of Additional Subsurface Investigation, dated January 8, 1999. <br /> In December 1999., ATC personnel supervised.the advancement of soil borings MW2, MW3, <br /> t and MW4 each to a depth of approximately 65 feet bgs. to. evaluate groundwater for the <br /> presence of petroleum hydrocarbons and to determine the groundwater gradient direction and <br /> nitoring well. Analytical data indicated that soil <br /> magnitude. Each boring was completed as a mo <br /> samples collectedfrom boring MW2 contained detectable concentrations of petroleum <br /> y hydrocarbons. Petroleum hydrocarbons were also detected in the groundwater sample <br /> collected from monitoring well MW2. A groundwater sample collected from MW3 contained very <br /> low concentrations'of only a few of the-,petroleum analytes. Petroleum.hydrocarbons were not <br /> detected in the groundwater sample obtained from MW4. Field activities and analytical results <br /> are summarized in ATC's Summary Report of Additional Subsurface Investigation, dated <br /> February 24, 2000: s <br /> In December 2001;, soil boring VEW1 was advanced to approximately 35 feet bgs, and borings <br /> VEW2 and VEW3 were each advanced to an approximate depth of 45 feet bgs. Borings MW5, <br /> MW6, and MW7 were each advanced to approximately 65 feet bgs and were completed as 2- <br /> inch diameter groundwater monitoring wells. .,;Soil borings VEW1, VEW2, and VEW3 were <br /> completed as 2-inch diameter vapor extraction wells. Boring CPT1 was advanced to <br /> approximately 100,feet bgs utilizing a truck-mounted Cone Penetrometer Testing (CPT) rig. <br /> In 2002, ATC performed a soil vapor extraction (SVE) pilot test using mobile- extraction <br /> equipment that yie'Ided a radius of influence (ROI) of approximately 30 feet at a vacuum of 11.5 <br /> inches of water. Approximately 2.64 pounds of total petroleum hydrocarbons were removed <br /> from the subsurface during the pilot test. Field activities and analytical results are presented in <br /> ATC's Remedial Investigation Feasibility Study dated November 19, 2002 <br /> From October 2004 to August 2006, ATC performed additional SVE system tests to provide <br /># information from which an efficient and.effective'permanent SVE system could be designed. <br /> I . <br /> In December 2006, ATC completed permitting and began installation of a SVE system with <br /> startup of the system occurring on January 17, 2007. The system continued operating until <br /> February 13, 2009, when volatile organic vapor concentrations betaine too low to justify <br /> sustained continuous operation. On July 14, 2009, after 151 days of non-operation, the SVE <br /> system was restarted in order to conduct a rebound test. Concentrations of volatile organic <br /> compounds (VOCs) measured from the influent air stream were determined to not significantly <br /> increased beyond the concentrations measured prior to the system shut down.in February 2009. <br /> The SVE system 1 rebound test supported historical data that indicated influent vapor phase <br /> hydrocarbon concentrations had decreased to -levels that, warranted terminating system <br /> operations. The:_test also .suggested that cycling the system would not be a cost effective <br /> alternative. <br /> i - <br /> During operation of the SVE system between; January 17, 2007 and February 13, 2009, the <br /> system operated for a total of 16,500 hours and successfully removed an estimated 5,436.76 <br /> pounds of total petroleum hydrocarbons as gasoline (TPHg), and an estimated 823.39 pounds <br /> SoilGasWorkPlan.doc 2 ATC Associates Inc. <br /> f <br /> i <br />