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ARCHIVED REPORTS_XR0002832
Environmental Health - Public
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2900 - Site Mitigation Program
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PR0508461
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ARCHIVED REPORTS_XR0002832
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Last modified
1/29/2020 4:26:56 PM
Creation date
1/29/2020 3:37:35 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0002832
RECORD_ID
PR0508461
PE
2950
FACILITY_ID
FA0008092
FACILITY_NAME
CONTINENTAL GRAIN CO
STREET_NUMBER
1805
STREET_NAME
HARBOR
STREET_TYPE
ST
City
STOCKTON
Zip
95203
APN
14502005
CURRENT_STATUS
01
SITE_LOCATION
1805 HARBOR ST
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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Appendix C by the boundaries of HA8, HA-9, the utility pole, and MW-3 The overburden area <br /> to removed and stockpiled for return to the excavation is estimated as 672 cubic yards—the same <br /> as in Alternative A2, however, in this altermtive, shoring is included to a depth of 28 feet and <br /> ' would cost between $85,000 and $95,000 Appendix C provides detailed information regarding <br /> this alternative <br /> ' Dewatering at a rate of 15 gpm is included and the extracted water would be treated with carbon <br /> prior to discharge to the City of Stockton sewer system Permits would be applied for this <br /> temporary discharge during excavation activities Costs for dewatering are consistent with the <br /> ' other two alternatives and are between$21,800 and $37,500 <br /> The soil removed (approximately 951 cubic yards) would be disposed of at a permitted landfill <br /> This option includes the addition of fill material equivalent to the volume taken off site <br /> An additional impediment to excavation is the 14 ft by 20 ft concrete pad, estimated to be 6 in <br /> thickness that is partially over the excavation area Half of this pad will have to be removed to <br /> allow excavation Costs for removing the concrete pad are estimated to be between $1,000 and <br /> $2,000 The power line and power pole that lay adjacent to the excavation area will also need to <br /> ' be removed for safety purposes The cost of removing the power line and power poll is <br /> estimated to be between $2,000 and $2,500 <br /> ' Soil sampling, project oversight, and removal of monitoring wells are all additional activities <br /> included in the cost estimate The shoring cost of$85,000 to $95,000 is a large component of <br /> the total cost estimated at $276,000 to $322,000 depending upon the volume of soil and water <br /> removed The total mass of hydrocarbon removed is estimated at 11,600 pounds of TPHd and <br /> TPH9 This is slightly more than Alternative Al and the costs are also higher by approximately <br /> ' two percent Cost per pound of TPH removed for this alternative is estimated to be between <br /> $23 73 and $27 70 <br /> Alternative A2 removes the soil source that has contributed to the appearance of free product and <br /> addresses the area of highest TPH concentrations in the soil The TPH plume is stable and will <br /> continue to slowly degrade over time and the addition of the calcium peroxide will also enhance <br /> the degradation process The time to achieve compliance cannot be differentiated between these <br /> alternatives as all three are removingapproximately 25 per cent of the total estimated mass of <br /> hydrocarbons This represents a consetvativd estimate as the dewatering process will also <br /> ' remove some of the hydrocarbon mass present in the groundwater <br /> 6. SUMMARY AND RECOMMENDATIONS <br /> ' Residual petroleum hydrocarbons measured as TPHd and TPHg in shallow groundwater in con- <br /> tact with the limited residual petroleum in,soil will likely remain above WQOs in a localized area. <br /> ' for a long period of time Removing the source of free product can be accomplished cost <br /> effectively by selecting Alternative A2 and conducting activities at the low water tables in <br /> August/September 2005 <br /> 19 <br /> RICONTGRANIStockton\CAPICAP ADDENDUM <br />
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