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ARCHIVED REPORTS_XR0002658
Environmental Health - Public
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3500 - Local Oversight Program
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PR0545259
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ARCHIVED REPORTS_XR0002658
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Last modified
1/31/2020 5:06:46 PM
Creation date
1/31/2020 3:15:17 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0002658
RECORD_ID
PR0545259
PE
3528
FACILITY_ID
FA0004966
FACILITY_NAME
CHEVRON USA (INACT)
STREET_NUMBER
45
Direction
E
STREET_NAME
HARDING
STREET_TYPE
WAY
City
STOCKTON
Zip
95204
APN
12707037
CURRENT_STATUS
02
SITE_LOCATION
45 E HARDING WAY
P_LOCATION
01
P_DISTRICT
002
QC Status
Approved
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SJGOV\sballwahn
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EHD - Public
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may be an over-estimate-due to- the fact that monitor well MW-5 1s _ - - <br /> not directly downgradient of MW-4 . <br /> K = Degradation Decay Rate = 2 . 303/t log(a/a-x) <br /> where: a = initial concentration = 101000 ppb - MW-4 , <br /> April 13 , 1989 <br /> a-x = reduced concentration = 2300 ppb - MW-5, <br /> July 12 , 1989 <br /> t = d/v = 30 ft/0. 02 ft/day = 1500 days <br /> 2 . 303 = constant of the equation <br /> K = 0. 001 days-' <br /> K = 0. 693/tin <br /> t112 = 593 days <br /> The degradation/attenuation decay rate is likely the product of a <br /> variety of processes, including biodegradation, dilution, <br /> adsorption, volatilization and abiotic chemical reactions such as <br /> hydrolysis. <br /> • 3) Calibration of the model <br /> Calculated maximum dissolved benzene concentrations expected in <br /> monitor well MW-3 ; assuming that MW-3 is directly downgradient of <br /> the presumed source, MW-4 . <br /> K = 2.303/t log(a/a-x) <br /> where: a = 10, 000-ppb - MW-4, April_ 13 , 1989 <br /> a-x = calculated reduced concentration, MW-3 <br /> t = d/v = 28 ft/0. 02 ft/day = 1400 days <br /> K = 0.001 days'' <br /> a-x = calculated maximum benzene concentration = 2580 ppb <br /> The maximum observed dissolved benzene concentration in MW-3 is <br /> 2700 ppb, measured on November 15, 1988. The similarity of the <br /> calculated benzene concentration with that observed in the well <br /> suggests that the derived degradation/attenuation rate is adequate <br /> for further calculations at the site. <br /> i <br /> 4 <br />
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