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ARCHIVED REPORTS_2010 ANNUAL REPORT
Environmental Health - Public
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ARCHIVED REPORTS_2010 ANNUAL REPORT
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Last modified
2/5/2020 8:37:32 PM
Creation date
2/5/2020 10:30:21 AM
Metadata
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Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
2010 ANNUAL REPORT
RECORD_ID
PR0009051
PE
2960
FACILITY_ID
FA0000649
FACILITY_NAME
FORMER NESTLE USA INC FACILITY
STREET_NUMBER
230
STREET_NAME
INDUSTRIAL
STREET_TYPE
DR
City
RIPON
Zip
95366
APN
25938001
CURRENT_STATUS
01
SITE_LOCATION
230 INDUSTRIAL DR
P_LOCATION
05
P_DISTRICT
005
QC Status
Approved
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Nestle USA, Inc., Ripon, California March 31, 2011 <br /> 2010 Annual Report <br /> equipment from damages, such as during power interruptions. The system was operational <br /> 95.9% of the time in 2010. The following is the breakdown of shutdown hours: <br /> • 108.5 hours due to high pressure at the City of Ripon NPS line; <br /> • 151.5 hours due to parts replacement (see description below); <br /> • 3 hours to replace a manufacturer's recalled part; <br /> • 3.5 hours for other repairs and maintenance; <br /> • 4 hours for system shut downs such as power failures due to weather. <br /> In addition to routine maintenance, the following activities were performed in 2010: <br /> • On March 4, 2010, the Stockton Avenue extraction and treatment system initiated a shut down <br /> due to flame loss. The system was non-operational between March 4 and March 10. ECM field <br /> technicians replaced a defective Veriflame controller that had been recalled. The Dungs gas <br /> solenoid valve failed due to water in the terminal box. ECM field technicians received a <br /> replacement part for the valve on March 10, 2010, installed the part and restarted the system to <br /> resolve the issue. The system operated without experiencing any similar events after the <br /> replacement. <br /> With approval from RWQCB, ECM stopped extraction from wells E-2 and E-6 and ceased <br /> system operation on October 1, 2010 (see Section 2.7). <br /> 4.2.2 PERFORMANCE MONITORING <br /> The Stockton Avenue extraction and treatment system featured two sampling points: <br /> • The influent to the air stripper (influent, combined flow from E-2 and E-6), <br /> • The effluent from the air stripper (discharge to the City of Ripon NPS). <br /> The influent to the Stockton Avenue extraction and treatment system included combined <br /> extracted groundwater from wells E-2 and E-6. <br /> COC concentrations for the combined influent to wells E-2 and E-6 decreased since 2004. TCE <br /> concentrations in the system influent declined to 16 pg/L, cis-1,2-DCE concentrations declined <br /> to 25 pg/L, and VC concentrations declined to 5.7 pg/L in 2010. <br /> The average mass removal rates of the Stockton Avenue extraction and treatment system have <br /> been declining, since extraction commenced in Upper Aquifer well E-2 in 2000, and in <br /> Intermediate Aquifer well E-6 in 2004. The rate of mass removal dropped from approximately <br /> 0.79 pounds per day during the First Quarter 2007 to 0.03 pounds per day during the Third <br /> Quarter 2010 due to reductions in E-6 flow rates and significant decrease in concentrations of <br /> COCs (Figure 12 and Figure 13). The reduced COC influent concentrations are consistent <br /> with a reduction in TCE concentrations in monitoring wells M-8A, M-8B and M-8C1 in this area <br /> (Appendix C). <br /> h The sustainable pumping rate for well E-6 dropped from an average of approximately 85 gpm during the First <br /> Quarter 2010 to 63 gpm during the Third Quarter 2010. Since September of 2006, the average annual <br /> sustainable pumping rate for E-6 decreased from 460 gpm to 76 gpm. <br /> 23 <br />
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