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' SOIL VAPOR EXTRACTION PILOT STOWORK PLAN � San oaquin County <br /> Montgomery Ward Auto Service Center Public Health Services Department <br /> 5400 Pacific Avenue, Stockton, CA Site Code 2163 <br /> samples obtained from borings 3 and 4 Total lead concentrations ranging from 6 to 36 ppm <br /> were present in all of the samples tested (see ADS, 1988) <br />' PHASE II INVESTIGATION (1991) <br />' In March 1991, Environmental Audit, Inc (EAI) drilled and sampled two borings (borings 13- <br /> 5 and B-6) at the Montgomery Ward site to determine whether operation of the former <br /> gasoline USTs impacted the environment (see Figure 2) Borings B-5 and B-6 were terminated <br /> at a depth of approximately 31 5 and 51 5 feet bgs, respectively Ground water was not <br />' encountered during drilling No total petroleum hydrocarbons as gasoline (TPH-G), benzene, <br /> xylenes or ethylbenzene were detected in any of the samples collected from boring B-5 (see <br /> Table 2) Toluene (ranging from 0 01 to 0 14 ppm) was the only aromatic hydrocarbon <br />' encountered in the samples obtained from boring B-5 Elevated concentrations of TPH-G, <br /> toluene, xylenes, and ethylbenzene were detected in seven of the ten samples obtained at <br /> depths from six to 50 feet bgs in boring B-6 (see Table 2) A solvent odor was noted during <br /> drilling of boring B-6 No organic lead was detected in any of the samples tested, and the <br />' TPH-G concentration in the sample collected at 50 feet bgs was 7 3 ppm The concentrations <br /> of total and organic lead detected were well below the standards contained in Title 22, <br /> California Code of Regulations (see EAI, 1991) <br /> PHASE III INVESTIGATION (1991) <br /> Sewer Line <br /> Montgomery Ward suspected that a broken sewer line may be the source of contamination in <br /> boring B-6 On June 9, 1991, Pacific Pipeline Survey (PPS) was retained by Montgomery <br />' Ward to investigate the existence of a possible break in the sanitary sewer manhole, associated <br /> piping, and a clarifier which are located in close proximity to the former location of the <br /> gasoline USTs According to this investigation, about one foot of the sewer line was broken <br />' On September 12, 1991, representatives of Stone Brothers excavated a trench around the <br /> suspected broken sewer line to an approximate depth of 2 5 feet bgs (see Figure 2) Two slant <br />' borings were drilled around the sewer line using a hand auger Commencing near the base of <br /> the clay pipe (2 5 feet bgs), slant boring SB-1 was hand angered to a calculated vertical depth <br /> of 5 75 feet bgs Two soil samples (SS-1 and SS-2) were collected from slant boring SB-1 at a <br /> depth of 3 5 and 5 5 bgs, respectively Slant boring SB-2 was hand augered to an estimated <br />' depth of 4 75 feet bgs in the sidewall of the excavation and a soil sample (SS-3) was collected <br /> at the termination depth The boring was terminated approximately beneath a second sewer <br /> line that extends west of the manhole <br /> 1 NT- 'I't)" iwr vo riatartari in nn�r Of the three Snil QnmT*)1PS agcnrintPd with the Sewer line �¢PP <br /> 11 V A 1 11 11—V �.F I�-l- \--- <br /> Table 3) However, minor concentrations of BTEX, bromoform, carbon disulfide, <br /> chloroform, tetrachloroethene, trichloroethene, 1,1,2,2-tetrachloroethane, 1,1,1- <br />' trichloroethane and 1,1,2-trichloroethane were detected in the soil samples tested (see Table 3 <br /> and EAI, 1991A) <br />' Project No 1232 A-2 ENVIRONMENTAL AUDIT, INC <br />