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Ms. Christina Carbajal <br /> April, 24, 2006 <br /> Page 4 <br /> SCS will continue to monitor and adjust all LFG extraction wells to minimize the amount of <br /> overpull while maintaining operational criteria. <br /> Also, on March 28,2006, SCS performed initial monitoring/adjustment to, recently installed by <br /> others,LFG Extraction.Well.Nos. FOFU-0304- Well, FOFU-04-06 through FOFU-04-12, FOFU- <br /> HCO1, FOFU-04-LCR,FOFU-05-06 and FOFU-OSHCI in.attempts to help decrease the observed <br /> elevated methane gas concentrations detected at GP-11 and GP-12 as directed by the client. SCS <br /> will continue to adjust wells as directed by Allied personnel.. <br /> Finally, during this reporting period,temperatures at LFG extraction wells were monitored and <br /> observed to range from 51 to 93 degrees Fahrenheit(see Table 3). These temperatures are <br /> considered to be in the low to normal range for anaerobic decomposition. SCS will continue to <br /> test LFG temperatures at each extraction well on a monthly basis in order to develop a database. <br /> This additional infoTmati.on should provide a better understanding of subsurface conditions at the <br /> site: - <br /> LFG Collection Systexn <br /> Visual observation of the LFG collection system.is conducted twice per month. During these <br /> visits, observations are made to ensure no pipe breakages have occurred and condensate drain <br /> sumps remain functional. Minor.repairs are completed as required. <br /> On March 8, 13, 21 and 27, 2006, SCS performed monitoring of all accessible LFG condensate <br /> 5u11Z.ps defined as ARTP-1 through 7 and FOTP-8 through 19 and recorded the liquid level control <br /> pump cycle counters (see Table 3)_ <br /> In addition, during pervious reporting periods, SCS observed and repaired several slight air supply <br /> and/or liquid leaks at several LFG condensate sumps. As requested by the Client, SCS has <br /> prepared a proposal dated August S, 2004,and recommends that the existing air and <br /> condensate connections he modified to decrease the potential for future separations/air leaks. <br /> Finally, SCS routinely conducts a pressure drop survey(Le., measurement of main pipeline <br /> pressure at various points throughout the LFG collection system). The results of this survey <br /> indicated that no major restrictions within the LFG collection system currently exist and all <br /> accessible extraction wells are receiving adequate vacuum. <br /> LFG Blower/Flare Station (BFS) <br /> Visual observations and testing of the LFG BFS was conducted on March 4. 8, 21, 22,23,27, 29 <br /> and 30. 2006. During these visits, operating parameters Axe zn.onitored and mechanical and <br /> electrical components are checked for workability. Throughout the.reporting period,the BFS was <br /> set to operate continuously. BFS data is shown in Table 4. <br />