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First Quarter 1994 Status Report March 31, 1994 <br /> Golden Grain Company, Manteca Bean Facility, 229 Moffat Blvd , Manteca, CA 4 <br /> The sod vapor extraction and groundwater treatment systems ran continuously this quarter except <br /> for four occasions The following is a list of the days that the remediation system was not <br /> operational <br /> 12/24/93 -01/03/94 The lead scrubber heater wires were burned and needed to <br /> be replaced The extended down time resulted from wanting <br /> for parts necessary to make repairs The wires burned as a <br /> direct result of the fuse block and solid state relay failure <br /> that occurred in September 1993 <br /> 01/07/94 - 01/10/94 Normal water build-up in vapor extraction underground <br /> pipelines filled the moisture knockouts and caused the <br /> system to shut down as a result increased vacuum and high <br /> pressure in the vapor system <br /> 02/08/94 System was automatically shut down as a result of a high <br /> LEL alarm condition The condition was traced back to <br /> moisture in the vapor lines which made the LEL sensors trip <br /> to an alarm condition <br /> 02/17/94 Normal water build-up within the underground vapor lines <br /> During this quarter of operation, there were no releases of untreated groundwater or untreated <br /> system effluent vapors System shutdowns were planned or triggered by the system interlock, which <br /> functioned as designed to bring complete system shutdown in the event of equipment malfunction <br /> Calculations using the TPH-G concentrations and system flow rates obtained during field visits <br /> indicate that approximately 245 pounds of TPH-G were removed from the sod by the vapor <br /> extraction system during this quarter The cumulative amount of hydrocarbons removed by the <br /> vapor extraction system since startup is estimated at 3,236 pounds Less than 1 pound of TPH-G <br /> was removed from the groundwater during this quarter Calculations for mass removal for the first <br /> quarter are included in Attachment 3 <br /> During this reporting period, the vapor treatment system was monitored each week The influent <br /> and effluent vapor concentrations were measured for TPH-G using an FID Values measured during <br /> site visits this quarter as well as historical data to July 1993 are shown in Table 3 The average <br /> destruction efficiency of 99 3 percent was calculated using weekly FID readings of the catalytic <br /> oxidizer effluent vapor stream for the operational period from December 10, 1993, through <br /> March 3, 1994 All effluent readings collected were below the 100 parts per million by <br /> volume (ppmv) TPN-G discharge limit specified by the Unified Air Pollution Control District permit <br /> (Permit No N-2625-1-0) to operate <br /> 55108014 020 <br /> GROUNDWATER <br /> TECHNOLOGY,INC <br />