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San Joaquin County DIRECTOR <br /> Environmental Health Department Donna Heran, REHS <br /> ASSISTANT DIRECTOR <br /> 600 East Main Street Laurie Cotulla, REHS <br /> :-K Stockton, California 95202-3029 <br /> PROGRAM COORDINATORS <br /> --- - - — Carl Borgman, REHS <br /> c Mike Huggins,REHS, RDI <br /> \ Margaret Lagorio, REHS <br /> FORr' <br /> Website: www.sjgov.org/�hd <br /> (209) 468-3420 Robert McClellon, REHS <br /> Fax: (209) 464-0138 Jeff Carruesco,REHS, RDI <br /> Kasey Foley, REHS <br /> THRIFTY OIL COMPANY NOV 3 0 2007 <br /> LARRY HIGINBOTHAM <br /> 13116 IMPERIAL HIGHWAY <br /> SANTA FE SPRINGS CA 90670 <br /> RE: Thrifty Station #172 RO#: 0557 <br /> 7647 Pacific Avenue CUF#: 002156 <br /> Stockton, CA 95207 Global ID#: T0607700504 <br /> The San Joaquin County Environmental Health Department(EHD) has reviewed Revised Work Plan <br /> for Well Abandonment, Replacement well installation, Reconfiguration of Conveyance Piping, and <br /> Interim Remedial Action by over Excavation in Conjunction with the UST System Removal(Plan) <br /> dated November 6, 2007, prepared by GeoHydrologic Consultants, Inc. (GHCI) for the above <br /> referenced site and has the following comments. <br /> This large revised proposal covers many aspects of field work the Thrifty Oil Company(TOC) is <br /> proposing to conduct during the month of November 2007. The original Plan dated August 7, 2007, <br /> was incomplete so the EHD required additional information. This Plan was submitted to meet those <br /> requirements. <br /> Wells"MW-12", "MW-11/VW-3"and"VW-2-S/VW-2-D"are in the current underground storage tank <br /> (UST) pit and TOC has proposed removing these wells in preparation for the UST removal. Two of the <br /> three wells are planned for replacement after the USTs are removed and the excavation is filled to the <br /> surface. Well MW-12 was constructed inside a steel conductor installed from the surface to 20-feet <br /> below grade. The over bore destruction proposal included in the Plan for this well is adequate and <br /> approved. <br /> The other wells were constructed with two PVC casings in a 10.5-inch bore hole and are also in a steel <br /> conductor casing from surface to 20-feet below ground surface('bgs). TOC has proposed pressure <br /> grouting both casings of each nested well with cement grout and then over-boring each before the <br /> grout sets to ensure that the casings are sealed in case the augers walk off the original borehole from <br /> 20'bgs to the total depth of original installation. The EHD has discussed well destruction procedures <br /> with Test America, the C-57 driller noted on the Well Permit Application Form submitted. The EHD <br /> has learned that Test America has steel rods that will fit inside the deep PVC of each nested well and <br /> that this will ensure the augers do not walk off the casing as the well is bored out. The EHD requires <br /> that rods be inserted in the deep casing of each nested well to total depth before the wells are bored <br /> out. Filling the casings with cement grout prior to over-boring is not necessary. The bentonite slurry <br /> proposed to be used to backfill the bored out wells is to be installed from total depth of the drill out to at <br /> least 10 bgs. This will allow for any settling of the material before the UST pit is over-excavated. <br /> The proposal to destroy the three wells noted above is approved with the conditions noted. (H&S Code <br /> 25296.10(c)(3)) <br />