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FOURTH QUARTER 2006 GROUNDWATER TREATMENT FACILITY MONITORING REPORT <br /> FORWARD LANDFILL WDR ORDER NO.R5-2003-0080 <br /> TABLE 1 <br /> Monthly Average Effluent Flow Rates <br /> Fourth Quarter 2111 Groundwater Treatment Facility Monitoring Report, <br /> Forward Landfill WDR Order No.R5-2003-0080 <br /> Average Flow Rate <br /> Month (gallons per day) <br /> October 313,000 <br /> November 360,000 <br /> December 281,000 <br /> At the beginning of fourth quarter 2006,both extraction wells were operational,and the <br /> effluent was discharging to the infiltration pond.The pressure gauge at EW-2 was replaced <br /> on October 12,2006. During the week of October 23,2006,additional metal barriers and <br /> sandbags were installed adjacent to EW-1 and EW-2 to divert runoff and prevent silt <br /> accumulation inside the concrete equipment vaults located at both wells. <br /> On October 30,2006,the submersible pump at EW-2 was observed to be cycling on and off, <br /> and the sample ports at both extraction wells were found to be leaking. On October 31,2006, <br /> both extraction wells were observed to be cycling on and off,and the GTF was shut down. <br /> The extraction well sample ports,the GTF influent sample port,and the GTF influent <br /> pressure gauge were replaced on October 31,2006. An electrician examined the GTF on <br /> November 3,2006,and determined that the cycling of the extraction well pumps was caused <br /> by disruption of the radio signals transmitted to the wells. <br /> After consulting with the manufacturer of the GTF radio controls,the GTF radio transmitter <br /> antenna and transmitter unit were replaced on November 9 and 13,2006,respectively.The <br /> GTF was restarted for continuous operation on November 13,2006.The pressure gauges at <br /> both extraction wells were replaced on November 16,2006,as a result of damage sustained <br /> during cycling of the submersible pumps. <br /> During fourth quarter 2006,intermittent outages occurred in the GTF autodialer telephone <br /> line.The wire to the AT&T telephone pole was replaced and the GTF phone conduit was <br /> repaired on November 9,2006. An electrician tested the GTF autodialer on December 1, <br /> 2006,and determined that the incoming AT&T phone line had failed. The telephone line <br /> was successfully repaired by AT&T on December 4,2006. A power outage occurred at the <br /> GTF on December 4, 2006,and the plant was restarted.The paddle wheel flow sensor at <br /> EW-2 was replaced on December 4,2006, and the sensor was rewired to the wellhead <br /> display panel. <br /> A power outage occurred at the GTF on December 10,2006,and the plant was restarted on <br /> December 11. The GTF experienced additional power outages on December 16 and 17,2006, <br /> and was restarted on December 18,2006. <br /> During inspections of the GTF on December 19 and 20,2006,wet soils were observed in the <br /> site access road approximately 400 to 450 feet east of EW-2. An elevated wellhead pressure <br /> was also observed at EW-2.On December 20,2006, EW-2 was shut off and the gate valve <br /> adjacent to EW-1 was closed to isolate the conveyance pipeline between EW-1 and EW-2. <br /> Shortly thereafter,the pressure in the pipe between EW-1 and EW-2 decreased to zero. <br /> According to these results,there appeared to be a leak in the buried groundwater <br /> RDD/070170002(NLH3358.DOC) 2 <br />